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Thread: Testing Motorola 280 ECM
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08-20-2021, 09:17 AM #16
I hope the other 5 are good! haha.
1973 Viper - sold
1978 Viking - sold
1995 XB02
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08-20-2021, 09:30 AM #17
Yeah me too. It sucks going through this
Hydrostream dreamin
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08-23-2021, 09:38 AM #18
We pulled the motor down all the way Sunday and I have top pinned pistons already so that is good. I asked the piston what happened and he said the ring broke. Well he was lying as as you can see the Pinocchio Piston was heated and stuck. I am guessing my water pump kit I installed came with china impeller!!! I am pulling the lower tonight to find out.
Me: "What happened Pinocchio Piston?"
Pinocchio: "Ring Broke"
Me: "Looks like you got hot."
Pinocchio: (says nothing and looks away....)
1973 Viper - sold
1978 Viking - sold
1995 XB02
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08-26-2021, 08:53 AM #19
OK. Mr Pinocchio piston may not be lying as my water pump looks really good as it only had about 15 hours on it. I could not see any issues with the water pump and gaskets were all good and intact. Maybe there was a ring failure?
1973 Viper - sold
1978 Viking - sold
1995 XB02
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08-26-2021, 09:44 AM #20
It got hot and that caused the ring failure.Can't trust pinocchio he's been hittin the sauce.
I may be slow but im ahead of you. *hit's only ankle deep but you went in head first.
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08-26-2021, 09:57 AM #21
I am going to look in my heads and flush those to see if there is anything in there. Nothing wrong or stuck in my water pump, water tube, adaptor plate. I did find some small pcs of plastic or rubber in the water jackets but not enough to fry a cylinder from lack of water.
1973 Viper - sold
1978 Viking - sold
1995 XB02
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08-26-2021, 11:05 AM #22
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08-26-2021, 11:10 AM #23
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08-26-2021, 11:19 AM #24
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I was referring to the side pinned one that loosed up and grab the port causing it to almost stick in the 800ft. runs
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08-26-2021, 12:45 PM #25
I though they were side pinned merc pistons before we pulled the motor, but once we pulled the motor apart we saw it was a good merc top pinned set of pistons already in the motor. I think I am going to swap my water tube from 1/2 to 3/4 inch to get some added volume. Also I am going to send #4 injector out as Brucato just cleaned them that same week the piston burnt! I had about 6-7 800 foot runs turning 9K+ before this happened. All the previous 10-15 hours on this motor was max of 8200 with the ROS ECM. I just got the unlimited ECM the day before the race and tested, worked well and per the prop calculator it ran 9600 on Friday using 9% slip, 29P, 2:1 lower. Then Saturday morning I did a run right before my races started and it only did 9400 so it was hurt by my race already I think..
1973 Viper - sold
1978 Viking - sold
1995 XB02
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08-26-2021, 02:38 PM #26
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You were running a 1/2 inch tube on a 1 piece adapter?
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08-26-2021, 03:13 PM #27
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And what lower unit?
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08-26-2021, 03:47 PM #28
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08-26-2021, 03:48 PM #29
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