User Tag List

Page 1 of 2 1 2 LastLast
Results 1 to 15 of 20
  1. #1
    Join Date
    Aug 2021
    Location
    Osteen/Deltona, FL
    Posts
    379
    Thanks (Given)
    42
    Thanks (Received)
    44
    Likes (Given)
    320
    Likes (Received)
    358
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)

    FF 200 after 50 hours on new rebuild

    We rebuilt this FF 200 after a major failure on cylinder #6 about 18 months ago for my buddy's 20ft Shadow tunnel bass boat. Two new sleeves, all machine work, all new components. Rebuilt the carbs after this failure as well, along with new fuel hoses and filters. Even cleaned out the fuel tank and added a water separator.

    Well yesterday on a straight run cruising about 45-50mph, 4,000 rpm or so it lost all power and stalled out. Cranked like it lost a few cylinders so we towed it back and pulled the heads. Although I told him which spark plugs to get when he went to service the boat, the auto parts store guy insisted he knew better with his "cross reference guide" It shouldn't have had Iridium's in it, but its too late now I guess lol.

    After such a thorough rebuild, my buddy is obviously devastated with the time and money lost. No damage the the cylinder walls, so its repairable but still. Obviously top two went lean, but damn... Any insight on something like this? Mixes 40:1 and it sure seemed like plenty of oil everywhere when we just pulled it apart yesterday. No Hot spots on the rods, bearings look perfect. I guess I am just trying to wrap my head around what went wrong.

    Click image for larger version. 

Name:	1and2.jpg 
Views:	64 
Size:	42.1 KB 
ID:	518943
    Click image for larger version. 

Name:	piston.jpg 
Views:	58 
Size:	46.1 KB 
ID:	518944
    Click image for larger version. 

Name:	plug.jpg 
Views:	72 
Size:	43.2 KB 
ID:	518945
    83 Vking 150 Mariner 2.5L






  2. #2
    Join Date
    Feb 2009
    Location
    Edgewater,B.C. CANADA
    Posts
    8,259
    Thanks (Given)
    179
    Thanks (Received)
    321
    Likes (Given)
    3578
    Likes (Received)
    1236
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Is it a Carb motor?

    Dave
    1980 Cougar 19 tunnel,90 2.4L Bridgeport EFI in middle of restoration.
    1988 BAJA Sunsport 186, 96 225 Pro Max
    79 12' Auminum, 95 Merc 9.9
    RIP Stu
    "So many idiots, so few bullets"

  3. #3
    Join Date
    Mar 2008
    Location
    Tourist Trap, Florida
    Posts
    14,753
    Thanks (Given)
    381
    Thanks (Received)
    1305
    Likes (Given)
    5602
    Likes (Received)
    11033
    Mentioned
    2 Post(s)
    Tagged
    1 Thread(s)
    Usually when the electrode goes poof, you have either heat (from wrong plug?) or timing went too high and caused detonation. jm2cts...

    83 V-King, 96 Mariner, 200 hp ff block 2.5 w/a 28p choppa
    We gotta clean this liberal mess up, VOTE TRUMP TO MAGA!
    Rebuild thread:
    http://www.screamandfly.com/showthre...-it&highlight=
    http://www.screamandfly.com/showthre...cs.&highlight=
    Videos

  4. Likes LakeFever, NICE PAIR liked this post
  5. #4
    Join Date
    Aug 2021
    Location
    Osteen/Deltona, FL
    Posts
    379
    Thanks (Given)
    42
    Thanks (Received)
    44
    Likes (Given)
    320
    Likes (Received)
    358
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Carb motor.

    Timing did come to mind, maybe those two had the highest numbers.
    83 Vking 150 Mariner 2.5L






  6. #5
    Join Date
    Jan 2020
    Location
    Pinole, Ca
    Posts
    2,273
    Thanks (Given)
    38
    Thanks (Received)
    285
    Likes (Given)
    927
    Likes (Received)
    878
    Mentioned
    4 Post(s)
    Tagged
    0 Thread(s)
    They do.
    Looks like an overheat or too much timing or both.
    I saw a 200carb run at 32deg timing for hella long.

  7. Likes OnPad liked this post
  8. #6
    Join Date
    Jun 2018
    Location
    Floating around
    Posts
    3,984
    Thanks (Given)
    474
    Thanks (Received)
    423
    Likes (Given)
    3393
    Likes (Received)
    2479
    Mentioned
    1 Post(s)
    Tagged
    0 Thread(s)
    My guesses

    1. Black boxes removed?
    2. Too much timing, too hot plugs
    2. crappy fuel Get some BND automotive ACES fuel additive
    3. Jetting to lean
    Hydrostream dreamin

  9. #7
    Join Date
    Feb 2009
    Location
    Edgewater,B.C. CANADA
    Posts
    8,259
    Thanks (Given)
    179
    Thanks (Received)
    321
    Likes (Given)
    3578
    Likes (Received)
    1236
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Quote Originally Posted by VkingMike View Post
    Carb motor.

    Timing did come to mind, maybe those two had the highest numbers.
    Some carbs have a lean spot aroung 4000rpm , the race carb 245hp motors were always rich to the point of almost 4 strokiing at that rpm to prevet lean burn down. First 225 Pro Max motors had an ECU recall for being lean at that rpm. Also water pressure and volume does a strang thing at that rpm due to poppet opening fully and the water pressure at that speed.
    Check timing on all cyl and set max timing on highest cyl. Make sure carbs are real rich at that rpm, replace the poppet.

    Dave
    1980 Cougar 19 tunnel,90 2.4L Bridgeport EFI in middle of restoration.
    1988 BAJA Sunsport 186, 96 225 Pro Max
    79 12' Auminum, 95 Merc 9.9
    RIP Stu
    "So many idiots, so few bullets"

  10. Likes LakeFever, rgsauger, CUDA liked this post
  11. #8
    Join Date
    Aug 2021
    Location
    Osteen/Deltona, FL
    Posts
    379
    Thanks (Given)
    42
    Thanks (Received)
    44
    Likes (Given)
    320
    Likes (Received)
    358
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Thanks guys, I'm going to help him get it back together and back on the water.

    The odd part is it ran hard and good for months on the river. Then BAM, this.
    83 Vking 150 Mariner 2.5L






  12. #9
    Join Date
    Mar 2004
    Location
    Brooklyn Park, MN
    Posts
    2,502
    Thanks (Given)
    29
    Thanks (Received)
    192
    Likes (Given)
    952
    Likes (Received)
    966
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    That should be a lesson to everyone! no part throttle running! Always WOT!
    1973 Viper - sold
    1978 Viking - sold
    1995 XB02

  13. Likes LakeFever, pcrussell50, rgsauger liked this post
  14. #10
    Join Date
    Aug 2021
    Location
    Osteen/Deltona, FL
    Posts
    379
    Thanks (Given)
    42
    Thanks (Received)
    44
    Likes (Given)
    320
    Likes (Received)
    358
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Quote Originally Posted by rjdubiel View Post
    That should be a lesson to everyone! no part throttle running! Always WOT!
    83 Vking 150 Mariner 2.5L






  15. #11
    Join Date
    Oct 2001
    Location
    MIAMI FLORIDA
    Posts
    2,290
    Thanks (Given)
    63
    Thanks (Received)
    124
    Likes (Given)
    359
    Likes (Received)
    759
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Those look like long reach plugs, heat range is one thing and it looks like a hot plug but also sticking the whole end of the plug into the chamber is a recipie for diaster... I would think he noticed that plug was much longer than the originals.

  16. Thanks KIRCHNER thanked for this post
    Likes David - WI, rgsauger, NICE PAIR liked this post
  17. #12
    Join Date
    Aug 2021
    Location
    Osteen/Deltona, FL
    Posts
    379
    Thanks (Given)
    42
    Thanks (Received)
    44
    Likes (Given)
    320
    Likes (Received)
    358
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Well, I am standing here looking over the disassembled engine and picked up the thermostats. They are full of what appears to be debris, grass, dried mud, etc. My now thought is he ran it shallow out of the ramp and sucked up trash.
    83 Vking 150 Mariner 2.5L






  18. Likes OnPad liked this post
  19. #13
    Join Date
    Jan 2020
    Location
    Pinole, Ca
    Posts
    2,273
    Thanks (Given)
    38
    Thanks (Received)
    285
    Likes (Given)
    927
    Likes (Received)
    878
    Mentioned
    4 Post(s)
    Tagged
    0 Thread(s)
    Very possible

  20. #14
    Join Date
    Mar 2022
    Location
    Lake Travis Texas
    Posts
    778
    Thanks (Given)
    20
    Thanks (Received)
    124
    Likes (Given)
    64
    Likes (Received)
    397
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Quote Originally Posted by H2OPERF View Post
    Those look like long reach plugs, heat range is one thing and it looks like a hot plug but also sticking the whole end of the plug into the chamber is a recipie for diaster... I would think he noticed that plug was much longer than the originals.
    Looks like it was much longer. SHould not see combustion on the threads.

    And never trust an auto parts counter guy on boat stuff.
    Jim

  21. Thanks rgsauger thanked for this post
  22. #15
    Join Date
    Aug 2006
    Location
    GA
    Posts
    855
    Thanks (Given)
    1
    Thanks (Received)
    25
    Likes (Given)
    35
    Likes (Received)
    71
    Mentioned
    2 Post(s)
    Tagged
    1 Thread(s)
    That Trash Can Do It..

  23. Likes FAST RALLY SPORT liked this post
Page 1 of 2 1 2 LastLast

Similar Threads

  1. best place for powerhead rebuild/lower rebuild on Long Island?
    By play2win in forum Technical Discussion
    Replies: 2
    Last Post: 08-08-2011, 01:49 PM
  2. 300 xs hours b-4 rebuild ??
    By Skater 32 in forum Four Stroke and Direct Injected Two Stroke Engines
    Replies: 8
    Last Post: 11-06-2009, 03:25 PM
  3. Hours until rebuild
    By Techno in forum Technical Discussion
    Replies: 17
    Last Post: 01-03-2003, 09:19 AM

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •  
Frank Mole Transport